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Re: Motor break- in, was SU setup for 1800cc

To: "Datsun Roadster List" <datsun-roadsters@autox.team.net>,
Subject: Re: Motor break- in, was SU setup for 1800cc
From: "Daryl Smith" <drlsmith@telus.net>
Date: Sun, 6 Nov 2005 21:11:43 -0800
Mike,
That would be a 50* discrepancy (210 to 160)! Was it running at 180*, which 
is near where it should be running?

What temp would be best to run at? My car has always run at about 190*, 
which is the midpoint of the gauge, so thought that was where it was 
supposed to be. If 180* or 170* would be better for power / efficiency, I 
can play with things to try to get it down there (thermostat, fan temp 
switch, etc.).

thanks
Daryl


----- Original Message ----- 
From: "datsunmike" <datsunmike@nyc.rr.com>
To: "Daryl Smith" <drlsmith@telus.net>; "Datsun Roadster List" 
<datsun-roadsters@autox.team.net>
Sent: Sunday, November 06, 2005 4:39 PM
Subject: Re: Motor break- in, was SU setup for 1800cc


> You should make sure the gauge is correct. That happened to me using and 
> aftermarket temp sender but in reality it was running at 160* rather than 
> an indicated 210*
>
> The guy who bought my car told me my temp gauge is off by 30* after he 
> tested the rad and rad hoses using an IR thermometer and a special tool he 
> has for his business and that's with a OEM sender and a fairly new gauge.
>
> 70lbs isn't bad - my car ran an estimated 60lbs.
>
> Mike
>
> ----- Original Message ----- 
> From: "Daryl Smith" <drlsmith@telus.net>
> To: "Datsun Roadster List" <datsun-roadsters@autox.team.net>
> Sent: Sunday, November 06, 2005 6:30 PM
> Subject: Re: Motor break- in, was SU setup for 1800cc
>
>
>> First off, Thank you for all the advice on first startup and breaking in 
>> the engine.
>>
>> Fired up the stroker last weekend, it sounded very good but, I had a 
>> couple of hiccups.
>>
>> 1. the exhaust manifold @ cylinders 2&3 only was turning a bright cherry 
>> red. I richened the mixture till it was not red. Forgot to check the 
>> timing, but pretty sure that is alright.
>>
>> 2. About the time I had the mixture richened the temp was hitting just 
>> over 200*, and the damn lower rad hose came off the rad! Anti-freeze and 
>> steam all over the place! The girlfreind came out figuring I'd blown it 
>> up!
>> Nobody scalded, no problems elsewhere, we checked it over and found some 
>> knucklehead had forgotten to tighten the clamp. (me) :-(
>>
>> 3. The GM temp switch I pulled from the wrecking yard ($2) didn't work so 
>> I had to rig up the electric fan to work manually until I get a working 
>> switch.
>>
>> 4. After refilling the cooling system, we fired it up for another try. 
>> Everything seemed to be going well. Good oil pressure (~70 psi @ 
>> 2200rpm), temp rising slowly, no leaks anywhere. hmm. Temp gauge kept 
>> rising slowly. Richened the mixture some more. About the time it hit 230* 
>> and was not coming down, even with the electric fan on we shut it down. 
>> Had to put it away for other commitments. !&%$##!!!!
>>
>> All told, somewhere between 10 and 15 minutes running time with both 
>> efforts.
>>
>> Checked it over a couple days later and had no coolant at the top of the 
>> rad, so I guess my efforts at "burping" it weren't good enough. Hoping to 
>> be able to give it another go sometime over the next week, if we get some 
>> decent weather. I'll top the rad off, check the timing, and probably 
>> richen the mixture a bit more for the next round.
>>
>> Any other suggestions welcome!
>>
>> On the positive side, I now know all my Classic Instruments gauges work 
>> (except for the speedo - no driving time yet). Tach works off the EDIS 
>> module CTO output. :-)
>>
>> Is 70 psi a little high for a stroker with a U20 oil pump? Running good 
>> quality 10W30 dino oil.
>>
>> Cheers
>> Daryl
>> '66 R series pain in the arse!




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